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That’s some rapid progress on the engine swap. Any news on the fate of your other engine?
No yet maybe get some info next week.
A little more progress today with engine mounts and inlet manifold fitted, checking out fitment of catch tank setup from other car.
Thanks, You still in the USA what happened to your 3b?
Well remembered! I swapped 4 years in the US and a convertible Mustang for coming back home to a NA Impreza and impending sidrick jr Imprezas are *****, by the way.
My old 3B, I'd love to know! Sold it to a local guy who seemed to love a project and had money to fling at it, but without really realising what these cars entail (no offence if you're reading). He e-mailed moaning months after the sale and I asked if he wanted to make it official (it was trailered away, had been started on front of him, and had no MOT) and never heard back. So I didn't want to chase it's next steps via him. I assumed it'd be sold and scrapped /facepalm. A real shame. I wish I'd stored it; nice little earner if I had kept it.
I loved that car. I love the S2, but I can't envisage buying another considering the price:ballache ratio that they are now, haha.
Managed to pick up a ABY fan cowling and motor for 3b but it was not spinning free.
Opened up motor as suspected brushes or bearing issue?
Turned out to be corroded spring clip for magnets which was a shame but maybe find a clip or at very least can get a new motor for plastic cowl.
​​​​​​​ ​​fan magnet clip broken.jpg
Continued rebuilding engine into 3b, as I was going to be fitting motronic ECU instead of VEMS had to do some alterations to get intake boot and MAF to fit.
Trimmed vertical bracket as intake boot was AAN configuration but fitted well after creating some space.
Opened up socketed ECU I got from Kit on the Forum to install EFI Express boost/fuel chips. Also MAP sensor and resistor mod completed.
Went to try a start but would only turn over but not fire? was worried about immobilizer being the issue but it turned out to be my fault as when I swapped to pins back from the flywheel sensor one of the wires was not clipped in correctly so after that it fired right up
Next I tried to bleed the clutch connecting ezebleed only to find the hose on the clutch cylinder had no clip on it.
It popped off under the dash with the pressure pumping Dot 4 into the drivers footwell
Once sorted got the cooling system bled and took out for test run.
Great feeling having it running again and will be able to continue on making it track worthy.
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Hopefully I am finally going to get to enjoy it and put some miles on the clock.
Got a few wee jobs when I get home but want to get out and drive it.
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Fit new slave cylinder
Fit AFR gauge
Seal coolerworks shifter with rubber gaiter underneath.
Rubber door trims
Head light trims
Carbon wrap roof again 3rd time lucky
Fix electric windows
Weld in drivers seat bars
Been making a list of current parts/spec
Engine
DNA Rebuild Wossner pistons, ZRP Rods
Gearbox
3b 5 speed with coolerworx shifter
Clutch
Sachs 707 pressure plate Disc RS4 Stg 3
Flywheel
12lb, 034 aluminum flywheel
Rear Diff
Torsen
Exhaust
3inch vee band downpipe to 2.75 2 box system
Intake
Wagner reverse with 8LS3 Throttle cable
Intercooler
Wagner with crossmember
Injectors
Siemens deka (630cc/min) injectors
Turbo
EFR 6758
Suspension
KW V1 coilovers AK motorsport solid top mounts
ARB RARB
Front standard S2 Rear whiteline
Bushes
Powerflex wishbone and subframe
Wheels
BBS RX 17 235/45/17
Wheel Spacers
15mm front 20mm back using 85mm studs
Exhaust manifold
Arlows RS2 rep K24 Flange
Engine management
Motronic 3bar MAP and resistor mod
Cooling
Aluminum radiator ABY fan
Fuel pump
Walbro 255
Seats
Bimarco bucket
Cage
Half Hoop Custom Cages/Scott Mcminn
Roof
welded sunroof /carbon wrap
Brakes
Vac Booster Porsche front with 328 A8 Discs Banbridge brackets
Rear Brakes
B7 Discs 300x22 vented A8/S8 Carriers Calipers from URS4 with S8 Pads
Some more work on the 3b
Got a new slave cylinder installed and bled.
Fitted a vems round car running 14.7 and about 12.6 on a cruise.
Needed to get the electric windows working as the drivers side was moving but making some nasty noises like it was going to snap any second.
Opened up the motor gear plate, the wire was all twisted and plastic wheel was toast.
Got a replacement cable and wheel on ebay so turned out to be an cheap fix.
The passenger side was not moving but was getting 12v and the motor was heating up so it was still alive, removed the two screws holding the motor and the motor jump in and out on the worm gear.
After that it started moving the window and freed off.
ABY block back from machine shop ready for rebuild.
Made a start cleaning the sump and oil pump.
Plan to assemble the bottom end and fit in the car first leaving cylinder head for later.
Need a second sump gasket as only received one in the kit.
Plan to put everything back original with dual mass flywheel and PCV system.
3b- Some small jobs off the list with modifying an V6 ECU bracket to get the ECU off the footwell.
Installed some new Lemforder front wishbones as my old ones were moving back and forth in the powerflex bushes, Think passenger side wishbone has had a bit of damage in the past so thought best to just buy two new ones.
Fitted an old set of bottom door trims to make it look a bit more respectable for MOT.
Got the alignment done for track use and passed the MOT
Been out for a few blasts and its really quick but was stalling at junctions?
No fault codes and output test confirmed ISV working, changed out ISV with another one I had and seems a lot better.
Finally got the car on a track day at Crail.
First time for me on this track as only been at Knockhill in the past.
I only had some issues at the end of the day with running a ABY fan on full speed as I dont have a resistor fitted so it was a bit much for the 40amp fuse.
Then on the way home it was getting harder to select a gear and the engine was stalling at junctions until the clutch stopped working in Dundee.
Fearing something had gone a miss with the clutch/release bearing my mate and I decided not wait about for recovery services but lock the S2 and drink our way back to Aberdeen on the train.
Great end to a day out
The next day once sober I hired a trailer to get it the last 60 miles home where I gravity bled the slave cylinder and the clutch started working again?
After reading back on my own thread, I remember I had a bit too much pressure on the ezibleed and popped the fluid hose off the master cylinder filling the foot well with fluid.
Maybe just trapped air as I never pumped the pedal while bleeding or ive damaged clutch master cylinder seals?
looks like my stalling issue was due to a dragging clutch.
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